The ALS RF systems, upgrades and ALS-U plans

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The ALS RF systems, upgrades and ALS-U plans M. Betz*, K. Baptiste, Q. Du, M. Vinco, S. Virostek 06/27/2018, CWRF2018, Hsinchu, Taiwan * mbetz@lbl.gov

Outline Structure of this talk RF systems in the Advanced Light Source (ALS) 2017-2018 work on the ALS storage ring RF Plans for the ALS-U RF 2

ALS-RF Overview 3

ALS-RF E-Gun 4 125 MHz from master oscillator hot deck @ -120 kv Heater PS Bias PS 25 W RF drive amp. (ENI 325) isolation transformer for mains supply Several optical links for control, monitor and RF Gating from timing system gun body analog optical link to drive amp on hot deck cathode of YU-171 triode Gun output 2.5 ns pulses

ALS-RF E-Gun & Linac E-Gun 125 MHz buncher RF power [kw] 3 GHz buncher 500 MHz buncher 24 Bunch length [ns] 2.50 Energy [MeV] 0.12 5 18 4000 0.80 0.20 3 GHz linac 1 3 GHz linac 2 16000 16000 0.02 0.01 25 50

ALS-RF E-Gun & Linac 6 LLRF 3 GHz waveguides In service since 1989, all analog proposing an upgrade to a digital FPGA based system Instrumentation e-gun 3 x buncher linac 1 linac 2 Wall current monitor Beam position monitors (buttons) Scintillator paddle with camera Switchable beam dump with Faraday cup

ALS-RF 125 MHz & 500 MHz buncher RF Tube amps LLRF Solid state amp Buncher cavity Eimac CV-2222 125 MHz cavity amplifier 125MHz: 5 x Eimac CV-2222 Pout ~24 kw for ~30 us 50 % power increase 500MHz: 5 x Eimac CV-2404 Pout ~18 kw for ~30 us 2018 Maintenance All 10 tubes replaced in 2018 Sockets cleaned of dust All amplifier cavities re-aligned 50 % increase in gain & output power with new tubes Eimac 3CPX800A7 Lifetime 10-12 years 7

ALS-RF 3 GHz buncher & linac RF 2 x Thales TV-2002 Klystrons 24 MW, 2us, 1 Hz, 50 W avg. In service: 1989 Klystron lifetimes [years] linac 1: 17, 10, linac 2: 9, 14, 2, 2+ 4+ Klystron Failures Internal parasitic emission Internal arcing Low / drifting output power 2013: collector water leak, fouled oil, shorted `buck coil` focusing magnet Modulator Failures Thyratron CX-1666 HV Caps HVPS & Cable 8 3 GHz waveguide (evacuated) klystron pulse forming network (PFN) focus magnet PSU focus magnet oil tank thyratron Replacement of PFN type modulator by a solid state type funded for FY18/19

ALS-RF Linac RF HV breakdowns Normal HV / RF pulsing 2018 frequent (every few days) modulator trips suspected arcing in the klystron oil shows signs of degradation, oil processing equipment on order might need to replace the tube soon 9 Pulses with suspected arcing PRF_IN Icathode Vcathode PRF_IN Icathode Vcathode persistence PRF_OUT PRF_OUT

ALS-RF 500 MHz booster RF Commercial IOT Based Broadcast TV Transmitter 10 Nominal operating parameters 6 ⅛ coax Vk = 32 kv Ik = 2.8 A Eff = 60 % Gain = 23 db Pout = 54 kw IOT lifetimes #1: 3 yrs failed due to poisoned cathode from HV cable fault #2: 9+ yrs Failures Grid Bias PS HV Cable fault (due to RF standing wave) HV Isolation Transformer Thyratron 2018: resistor went open circuit in analog LLRF system HV modulator / crowbar IOT CPI K2H80W output resonator assembly

ALS-RF Storage ring RF 11 Klystron Operating Parameters Vk = -53.1 kv Ik = 9.55 A Va = 32.8 kv Ia = 1.6 ma Eff = 51.53% Gain = 41.41 db μp = 1.61 RF Output = 261.7 kw Wg. switch matrix RF system Operational since 2012 Nominal RF output power ~260 kw with a single klystron (500 ma, nominal ID gap) In 2019: ~360 kw max. with 2 klystrons Kly. 2 Issues HV filter capacitor degradation Arc detectors not reliable (due to ionizing radiation!) Mod anode control system... Kly. 1 Thales 2161L IGBT HV. SW. Mod. anode hot deck

ALS-RF Storage ring RF 12 Filament PSU HV PSU PLC I/O module hot deck, floating at Vcath -55 kv Since 2012, intermittent loss of filament current / mod anode voltage trip of klystron interlock system ( ~ once a month) Problem really surfaced in 2017 (several trips a day!) plastic fibres Main PLC By installing a `Lab-Jack` DAQ module we could narrow down the faulty behavior to the PLC I/O module Proprietary digital link over plastic fibres One fiber was found partly damaged bad enough to cause I/O glitches due to `bit errors` not bad enough for the PLC to signal a link error

ALS-RF Storage ring RF Wg. Switch Matrix Provides operational redundancy Operating modes Kly. 1 or 2 single drive (shown) Dual drive Dummy load drive Cavity to test port for VNA meas. Current state Wg. switches locked in place as shown 2019: finish work on control / interlock system for full 2 klystron operation 13

SRRF Reliability - Beam time lost 14

SRRF Reliability - Mean time between faults 15

SRRF Reliability - Mean time to recovery 16

SR-RF upgrades Timeline 17 New HVDC power supply Finished waveguide switch-matrix RF phase noise improvements 2013 2016 2018 2012 2014 2017 2019 Established Klystron site #2 Installed IGBT based disconnect switch Commissioned digital LLRF system Full 2 Klystron operation

SR-RF upgrades Digital LLRF 18 Hardware Xilinx KC705 eval. board (Kintex 7) + ADC & DAC daughter boards by 4DSP Custom made 500 MHz up / down converter board Features Scalable, distributed design, 42 input / output channels with 60 MHz bandwidth 1.45 μs interlock latency Non - IQ sampling Managed through gigabit ethernet interface Epics integration / python expert GUI Open Source! Code available on github In progress FMC112 Narrow-band network analyzer feature System-on-a-chip for initialization & housekeeping Timing system integration (Micro-research Finland) SRRF loop optimization (avoid `fighting` with ALS longitudinal feedback) KC705 FMC150 multi-channel up / down converter RF phase step response with 500 ma nominal beam

SR-RF upgrades Phase noise hunting 19 MO replacement selected & ordered 3.75 khz Significant improvement for IR beamline users Replaced in 2018 Upgrade of coax based MO distribution system in conceptual design stage Old amp. New amp.

Overview > 100 fold increase in soft x-ray brightness Requires new lattice in the storage ring, diffraction limited emittance Unique: on axis swap out injection to satisfy the smaller dynamic apertures of the new lattice Storage ring New accumulator ring for topping-up the swapped-out bunch train Beam profile ALS - U 20 ALS ALS-U Plans ALS ALS-U Accumulator new reused Storage ring

ALS-U Plans Cavities Storage ring 21 Accumulator There is a real chance of reusing the existing 500 MHz ALS RF system + cavity But optimum coupling factor ~10, existing coupler only achieves < 3.2 Option 1 live with reflected RF power (and larger electricity bill) Option 2 develop a new RF coupler Simulation work in progress Severe space constraints will need to modify the concrete shielding Exploring existing cavity options ALS SRRF cavity Research Instruments - EC Dampy cavity Toshiba ASP cavity RF Performance & Cooling: RI & Toshiba have no big differences Fit: Toshiba cavity would be a leading candidate if coupler coaxial section is extendable. NDA? ceiling Cylindrical RF window in wg. coupling iris ALS SR cavity ALS SR cavity RI - EC cavity Toshiba cavity

ALS-U Plans 2 amplifiers (one for each cavity) optional: 3rd amplifier to improve reliability (might not be needed with SSAs) simplified switch matrix Accumulator RF 22

ALS-U Plans Accumulator RF Example: VHF solid state amplifier for the LCLS-II Gun B collaboration Major specs. CW output power [kw] Frequency [MHz] 1 db bandwidth [MHz] 23 60-80 499.6 Two 60 kw CW SSA at 186 MHz preparing for test at factory >4 Additionally, we would like High Reliability / Fault Tolerance: continue to operate with N failed transistors, amp. modules or power supplies (PS) Maintenance: modular design, dripless quick disconnects, hot-swappable DC PS Fail-Safe Controls & Interlocks can be met by commercial SSA s See poster by K. Baptiste on Thursday

Booster IGBT magic-smoke was released Booster Bend Magnets 1 cycle per second 1.2 MJ capacitor bank for energy storage between cycles 24 Magic smoke Power converter based on Semikron IGBT bridge modules rated 1.7 kv, 2.4 ka, switches @ 2 khz 11. April 2018 upper half-bridge switch failed closed during its conduction period, root cause not clear short across the DC bus in the next half-cycle IGBT module went through rapid unscheduled disassembly 12 x 100 A fuses blew in the cap. bank and prevented worse replacing IGBT module and a DC bus filtering cap. allowed us to start back up Capacitor bank failed IGBT module

Booster IGBT magic-smoke was released 25 4 x IGBT arrays on cold-plate IGBT dies failed short failed short arcing damage on back of a failed module burned bus bar / transducer

Summary 26 The injector and its RF systems will still be needed for a long time. Legacy systems are being replaced step by step. (S-Band PFN modulators, analog LLRF, etc.) Storage ring RF system upgrade very close to completion (Outstanding: Arc detector issues, control and interlock integration for second klystron) There s a good chance we will need a new solid state amplifier + cavity for the ALS-U accumulator ring soon

27 Thank you!

ALS-RF Booster cavity 28 Coax to wg. trans. WR1800 waveguide Center Frequency Harmonic # Peak acc. voltage (@ 66 kw) 499.64 MHz 125 Iris flange WR1800 waveguide 813 kv Beam current (multibunch) 4 ma Synch. rad. loss (dipoles) 5 kw Shunt imp. (ZT2) 5 MΩ RF power required Cylindrical ceramic window Beam port HOM port 54 kw beam loading + cavity loss + return loss + transmission loss RF power installed 80 kw Piston tuner