Dramatic Vibration Improvement due to Ring-Section Pump Foundation Repair Based on ODS in a Power Plant

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Dramatic Vibration Improvement due to Ring-Section Pump Foundation Repair Based on ODS in a Power Plant 26 th International Pump Users Symposium March 15-18, 2010 By: Maki M. Onari Mechanical Solutions, Inc. William Hausman Constellation Energy Mark Fry Hydro East, Inc.

History Three multistage ring-section BFP s installed in 1991 at Panther Creek Energy Waste Coal-Fired Power Plant (83 MW). Pumps driven by two-pole induction motors (3,585 rpm or 59.8 Hz). In 2007, Pump #2 was removed for maintenance service after nine years of continuous operation. Normal vibration below 0.10 in/s peak @ 1x rpm.

History Detected high vibration at the outboard bearing housing in the horizontal direction. Gradual vibration increment over time (from 0.06 in/s pk to 0.25 and 0.35 in/s pk). Over one year period, modifications were implemented to improve the erratic vibration amplitude: - Motor and pump pedestal pads machined to eliminate alignment shims under pump. - Spare rotor assembly was balanced with 1W/N spec. and installed in the pump. - Sleeve bearings were replaced due to high bearing temperature.

Vibration Testing Monitoring test during transient and steady operation to monitor the vibration amplitude, natural frequencies, and phase angle. Experimental Modal Analysis (EMA) test to determine the natural frequencies of the pump structure and the rotor system. Operating Deflection Shape (ODS) testing during steady operation.

Vibration Monitoring Pump #1 Typical Spectrum OBB in the Horizontal Direction [g] 100m 30m Autospectrum(Signal 17) - Mark 1 (Magnitude) Working : ODS 1 Rec 0 : Input : FFT Analyzer 1x rpm (0.06 in/s peak) 3m 300u 30u 10u 0 20 40 60 80 100 120 140 160 180 200 Natural frequency at 67.3 Hz (12.6% above 1x rpm)

Vibration Monitoring Pump #3 Typical Spectrum OBB in the Horizontal Direction [g] 1 Autospectrum(Signal 17) - Mark 1 (Magnitude) Working : ODS 49 Rec 16 : Input : FFT Analyzer 1x rpm (0.17 in/s peak) 100m 10u 0 20 40 60 80 100 120 140 160 180 200 Natural frequency at 68 Hz (13.8% above 1x rpm)

Vibration Monitoring Pump #2 Typical Spectrum OBB in the Horizontal Direction [g] 1 Autospectrum(Signal 17) - Mark 1 (Magnitude) Working : Shaft Stick Triax 1 and 2 Repeated Good Rec 53 : Input : FFT Analyzer 1x rpm (0.23 in/s peak) 100m 10u 0 20 40 60 80 100 120 140 160 180 200 Closest Natural frequency at 56.8 Hz (5% below 1x rpm)

Vibration EMA Test Pump #2 Modal (Operating) Spectrum in the Horizontal Direction at the Pump OBB Housing [g/lbf] Frequency Response(Signal 3,Signal 17) - Mark 1 (Magnitude) Working : Modal 4 Horiz Rec 2 : Input : Enhanced 1xN 3m 300u 30u 10u 3u 1u Rotor natural frequency? (Backwards precession) Rotor natural frequency? (Forward precession) Structural. natural frequency 0 20 40 60 80 100 120 140 160 180 200 Closest Natural frequency at 56.8 Hz (5% below 1x rpm)

Operating Deflection Shape Natural excitation signature of the pump structure. Over 850 vibration measurements. Data base of amplitude vs. frequency and phase angle. 3-D CAD model assigning motion to each individual vibration data point. Create animations of the pump

Operating Deflection Shape Baseline data Pump #2 @ 1x rpm

Operating Deflection Shape Pump #2 @ 1x rpm after OB feet bolts tightened

Operating Deflection Shape Pump #2 @ 1x rpm after OB feet bolts tightened

Operating Deflection Shape Actions Taken: All J-bolts of the baseplate torqued up to 600 ft-lb. Pump IB feet bots torqued up to 1000 ft-lb. Dowel pin and holes cleaned up and drove pins in tight. Pump OB feet tightened after full warm-up condition

Operating Deflection Shape Pump #2 @ 1x rpm after OB feet bolts and baseplate anchor bolts tightened

Vibration Monitoring Pump #2 Typical Spectrum OBB in the Horizontal Direction [g] 100m Autospectrum(Signal 17) - Mark 1 (Magnitude) Working : Linear Steady : Input : FFT Analyzer 0.06 in/s peak 57 Hz Time: 9:50 64.5 Hz 10u 1u [g] 100m 0 20 40 60 80 100 120 140 160 180 200 Autospectrum(Signal 17) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 0.35 in/s peak Time: 14:04 62.8 Hz 10u 1u 0 20 40 60 80 100 120 140 160 180 200

Vibration Monitoring Pump #2 OBB Housing Vibration Trend in the Horizontal Direction BFP Pump #2 OB Bearing Horizonal Vibration at 1x rpm (59.8 Hz or 3585 rpm) Vibration Amplitude (in/s peak) 0.400 0.350 0.300 0.250 0.200 0.150 0.100 0.050 0.000 9:45 9:50 9:55 10:00 10:05 10:10 10:15 10:20 10:25 10:30 10:35 10:40 10:45 10:50 10:55 11:00 14:10 14:15 14:20 ODS Test Tine

Vibration Monitoring Pump #2 Proximity Probe Phase Angle Trend Plot BFP Pump #2 Proximity Probe Phase Angle at 1x rpm (59.8 Hz or 3585 rpm) Phase Angle (Degrees) 50 0-50 -100-150 -200-250 -300 9:45 9:50 9:55 10:00 10:05 10:10 10:15 10:20 10:25 10:30 10:35 10:40 10:45 10:50 10:55 11:00 14:10 14:15 14:20 ODS Test Time OBX OBY IBX IBY

Vibration Monitoring Pump #2 Shaft Orbits at 14:20 (4.5 hours after cold start up) OBB IBB 6.5 mils pk-pk 2.5 to 3.0 mils pk-pk

Vibration Monitoring Pump #2 Shaft Spectra at 14:20 (4.5 hours after cold start up) [mil] 10 Autospectrum(Signal 13) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 4.8 mils pk-pk OBX [mil] 1 Autospectrum(Signal 15) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 1.6 mils pk-pk IBX 1 100m 100m 10u 0 100 200 300 400 500 600 700 800 0 100 200 300 400 500 600 700 800 [mil] 10 1 Autospectrum(Signal 14) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 5.0 mils pk-pk OBY [mil] 100m Autospectrum(Signal 16) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 1.2 mils pk-pk IBY 100m 10u 0 100 200 300 400 500 600 700 800 0 100 200 300 400 500 600 700 800

Vibration Monitoring Pump #2 Shaft Proximity Probe - OBY Spectra [mil] 1 Autospectrum(Signal 14) - Mark 1 (Magnitude) Working : Linear Steady : Input : FFT Analyzer 300m 100m Time: 9:50 30m 3m 57 Hz 300u [mil] 10 0 20 40 60 80 100 120 140 160 180 200 Autospectrum(Signal 14) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 3 1 Time: 14:04 300m 100m 30m 3m ~60 Hz 0 20 40 60 80 100 120 140 160 180 200

Preliminary Conclusions 1. Excessive flexibility at the baseplate due to possible softness or delamination of the internal grout (Pump #2 moved 10x more than Pump #1). 2. OBB housing vibration increased almost 6 times in 4 hours of operation (from 0.06 in/s peak to 0.35 in/s peak @ 1x rpm), and 50% shaft vibration. 3. During the cold start up, 1x rpm spike located between two natural frequencies (57 Hz from the rotor lateral and 63.5 Hz from the structure). The structure became less stiff and reducing the damping of the system; therefore, the rotor natural frequency shifted upwards in the neighborhood of the running speed. 4. Shaft phase angle variation over time. (OBX -60 deg., OBY -20 deg., IBX -110 deg., and IBY -110 deg.) 5. Pumps #1 and #3 did not indicate rotor natural frequencies near the running speed. The lateral rocking mode was identified 13% above 1x rpm.

Proposed Recommendations 1. Inspect the welding areas of the pedestal and the baseplate for potential cracks. 2. As a short term fix, increase the stiffness of the baseplate. 3. As a long term fix, the baseplate should be regrouted to assure rigid connection with the foundation and proper structural damping.

Pump Pedestal & Baseplate Modifications

Vibration Monitoring Pump #2 Typical Spectrum OBB in the Horizontal Direction After Implementing Modifications [g] Autospectrum(Signal 3) - Mark 1 Working : Linear Ave Before ODS : Input : FFT Analyzer 1 100m 1x rpm (0.09 in/s peak) 10u 0 20 40 60 80 100 120 140 160 180 200 Natural frequency at 73 Hz (23% above 1x rpm)

Vibration EMA Test Comparison of FRF from EMA Test (not Operating) in the Horizontal Direction at the Pump OBB Housing [g/lbf] Frequency Response(Signal 2,Signal 17) - Mark 1 (Magnitude) Working : Horiz 1 Rec 0 : Input : Enhanced [g/lbf] Frequency Response(Signal 3,Signal 7) - Mark 1 (Magnitude) Working : OBB Horiz Hits Sig 3 : Input : Enhanced 3m 3m 300u 300u 30u 10u Running Speed 30u 10u Running Speed 3u 3u 1u 1u 0 20 40 60 80 100 120 140 160 180 200 0 20 40 60 80 100 120 140 160 180 200 Before After

Vibration Monitoring Pump #2 Proximity Probe Phase Angle Trend Plot After Implementing Modifications BFP Pump #2 Proximity Probe Phase Angle at 1x rpm (59.8 Hz or 3585 rpm) 350 Phase Angle (Degrees) 300 250 200 150 100 50 0 11:31 11:45 12:00 12:14 12:28 12:43 12:57 13:12 13:26 13:40 13:55 14:09 Time OBB X OBB Y IBB X IBB Y

Vibration Monitoring Pump #2 Shaft Spectra Before and After Implementing Modifications [mil] 10 1 Autospectrum(Signal 14) - Mark 1 (Magnitude) Working : Linear Steady After ODS & DP : Input : FFT Analyzer 4.8 mils pk-pk Before 100m 0 100 200 300 400 500 600 700 800 [mil] Autospectrum(Signal 15) - Mark 1 Working : Linear Ave Before ODS : Input : FFT Analyzer 1 300m 100m 1.6 mils pk-pk After 30m 3m 300u 0 100 200 300 400 500 600 700 800 26 th International Pump Users Symposium Case Studies

Final Operating Deflection Shape

Conclusions The root cause of the vibration on Pump #2 was due to excessive flexibility at the baseplate caused by softness or delamination of the internal grout. This phenomenon originated due to the looseness of the anchor J-bolts. After all modifications performed on the baseplate, the maximum vibration amplitude at the OBB housing in the horizontal direction was reduced from 0.35 in/s peak to a greatly improved value of 0.09 in/s pk @ 1x rpm. The ODS is a powerful troubleshooting tool to facilitate and visually understand most common vibration problems in any pumping system or turbomachine.

Thank you Any Questions?