Review of Diamond SR RF Operation and Upgrades

Similar documents
IOT OPERATIONAL EXPERIENCE ON ALICE AND EMMA AT DARESBURY LABORATORY

Status of SOLARIS. Paweł Borowiec On behalf of Solaris Team

Dark current and multipacting trajectories simulations for the RF Photo Gun at PITZ

Experience with the Cornell ERL Injector SRF Cryomodule during High Beam Current Operation

!"!3

ANKA RF System - Upgrade Strategies

Operating Experience and Reliability Improvements on the 5 kw CW Klystron at Jefferson Lab

3 cerl. 3-1 cerl Overview. 3-2 High-brightness DC Photocathode Gun and Gun Test Beamline

Detailed Design Report

RF Power Generation II

SLS RF operation report 2003

RF plans for ESS. Morten Jensen. ESLS-RF 2013 Berlin

IOT RF Power Sources for Pulsed and CW Linacs

Status of BESSY II and berlinpro. Wolfgang Anders. Helmholtz-Zentrum Berlin for Materials and Energy (HZB) 20th ESLS-RF Meeting

A HIGH POWER LONG PULSE HIGH EFFICIENCY MULTI BEAM KLYSTRON

SRS and ERLP developments. Andrew moss

RF Solutions for Science.

NSLS-II RF Systems James Rose, Radio Frequency Group Leader PAC 2011

High Brightness Injector Development and ERL Planning at Cornell. Charlie Sinclair Cornell University Laboratory for Elementary-Particle Physics

TECHNICAL SPECIFICATION Multi-beam S-band Klystron type BT267

RF Upgrades & Experience At JLab. Rick Nelson

Chris Gilmour Studies into the Design of a Higher Efficiency Ku Band ring-loop Travelling Wave Tube SWS using the CST PIC Software.

Investigation of Radio Frequency Breakdown in Fusion Experiments

Evaluation of Performance, Reliability, and Risk for High Peak Power RF Sources from S-band through X-band for Advanced Accelerator Applications

North Damping Ring RF

DESIGN AND PERFORMANCE OF L-BAND AND S-BAND MULTI BEAM KLYSTRONS

Spear3 RF System Sam Park 11/06/2003. Spear3 RF System. High Power Components Operation and Control. RF Requirement.

Linac 4 Instrumentation K.Hanke CERN

RF considerations for SwissFEL

Diamond RF Status (RF Activities at Daresbury) Mike Dykes

Pseudospark-sourced Micro-sized Electron Beams for High Frequency klystron Applications

Mechanical aspects, FEA validation and geometry optimization

The LEP Superconducting RF System

Proceedings of the 1997 Workshop on RF Superconductivity, Abano Terme (Padova), Italy

Optical Cryostat - Omniplex TM

45 MW, 22.8 GHz Second-Harmonic Multiplier for High-Gradient Tests*

Design, Fabrication and Testing of Gun-Collector Test Module for 6 MW Peak, 24 kw Average Power, S-Band Klystron

KARA and FLUTE RF Overview/status

Experimental Results of the Coaxial Multipactor Experiment. T.P. Graves, B. LaBombard, S.J. Wukitch, I.H. Hutchinson PSFC-MIT

Guided Wave Radar Level Meter

INFN School on Electron Accelerators. RF Power Sources and Distribution

Recent APS Storage Ring Instrumentation Developments. Glenn Decker Advanced Photon Source Beam Diagnostics March 1, 2010

Thyratrons. High Energy Switches. Features. Description

Drift Tubes as Muon Detectors for ILC

DEVELOPMENT OF A 10 MW SHEET BEAM KLYSTRON FOR THE ILC*

X-Band Klystron Development at

TOSHIBA Industrial Magnetron E3328

Synchrotron Light Facility. Operation of ALBA RF. Angela Salom on behalf of RF team: Francis Perez, Bea Bravo and Jesus Ocampo

An extreme high resolution Timing Counter for the MEG Upgrade

14 GHz, 2.2 kw KLYSTRON GENERATOR GKP 22KP 14GHz WR62 3x400V

IOT Charakterization at BESSY ( HZB)

RF Power Klystrons & 20 Year Look. R. Nelson 7/15/15

TEST RESULTS OF THE 84 GHZ / 200 KW / CW GYROTRON

18 GHz, 2.2 kw KLYSTRON GENERATOR GKP 24KP 18GHz WR62 3x400V

Pulsed Klystrons for Next Generation Neutron Sources Edward L. Eisen - CPI, Inc. Palo Alto, CA, USA

Technology Challenges for SRF Guns as ERL Sources in View of Rossendorf work

The Elettra Storage Ring and Top-Up Operation

PEP-I1 RF Feedback System Simulation

Development of Multiple Beam Guns for High Power RF Sources for Accelerators and Colliders

220KV EHV NETWORK AT RELIANCE JAMNAGAR REFINERY COMPLEX

Jefferson Lab Experience with Beam Halo, Beam Loss, etc.

AREAL- Phase 1. B. Grigoryan on behalf of AREAL team

LITTON IOT CIRCUIT ASSEMBLY MANUAL

Beam Loss Detection for MPS at FRIB

The ESS Accelerator. For Norwegian Industry and Research. Oslo, 24 Sept Håkan Danared Deputy Head Accelerator Division Group Leader Beam Physics

CPI Gyrotrons For Fusion EC Heating

RF PERFORMANCE AND OPERATIONAL ISSUES

Preparations for Installation, Testing and Commissioning based on Experience at CERN, SNS and Siemens

TWO BUNCHES WITH NS-SEPARATION WITH LCLS*

Commissioning of Accelerators. Dr. Marc Munoz (with the help of R. Miyamoto, C. Plostinar and M. Eshraqi)

THERMIONIC GUN CATHODE-GRID ASSEMBLY TEST PROCEDURE

New Filling Pattern for SLS-FEMTO

ARES Status 2004(JFY)

L-Band RF R&D. SLAC DOE Review June 15 th, Chris Adolphsen SLAC

Status of SOLARIS Arkadiusz Kisiel

Commissioning the TAMUTRAP RFQ cooler/buncher. E. Bennett, R. Burch, B. Fenker, M. Mehlman, D. Melconian, and P.D. Shidling

3B SCIENTIFIC PHYSICS

TIL311 HEXADECIMAL DISPLAY WITH LOGIC

Effects of the cryogenics operational conditions on the mechanical stability of the FLASH linac modules

Optical Cryostat - Economy

Bunch-by-bunch feedback and LLRF at ELSA

Summary of CBETA Independent Cost Reviews. R. Michnoff January 19, 2017

Particle-in-cell simulation study of PCE-gun for different hollow cathode aperture sizes

Development of high power gyrotron and EC technologies for ITER

4.9 BEAM BLANKING AND PULSING OPTIONS

CX1725W Liquid Cooled, Hollow Anode Two-Gap Metal/Ceramic Thyratron

Present Status and Future Upgrade of KEKB Injector Linac

Pulses inside the pulse mode of operation at RF Gun

A New 4MW LHCD System for EAST

Closed Cycle Cryogenic Probe Station

4.4 Injector Linear Accelerator

CHAPTER 4: HIGH ENERGY X-RAY GENERATORS: LINEAR ACCELERATORS. Jason Matney, MS, PhD

News from HZB / BESSY Wolfgang Anders at ESLS-RF Meeting September 2010 Trieste

K800 RF AMPLIFIER TUBE UPGRADE

PoS(EPS-HEP2015)525. The RF system for FCC-ee. A. Butterworth CERN 1211 Geneva 23, Switzerland

GENCOA Key Company Facts. GENCOA is a private limited company (Ltd) Founded 1995 by Dr Dermot Monaghan. Located in Liverpool, UK

SLAC-PUB-2380 August 1979 (A)

Modifying the RW1127 and similar TWTs for 24GHz

GA A26497 SOLID-STATE HIGH-VOLTAGE CROWBAR UTILIZING SERIES-CONNECTED THYRISTORS

High-power klystrons. The benchmark in scientific research. State-of-the-art RF sources for your accelerator

Transcription:

Review of Diamond SR RF Operation and Upgrades Morten Jensen on behalf of Diamond Storage Ring RF Group

Agenda Stats X-ray and LN2 pressure results Cavity Failure Conditioning in the RFTF Cavity Simulations IOT Upgrade Helium Refrigerator update

MTBF and Number of trips MTBF and Number of trips 180.0 160.0 140.0 120.0 100.0 80.0 60.0 40.0 20.0 0.0 38 RF MTBF of beam loss and Number of beam trips per run 18 21 26 18 6 21 20 12 36 c 13 15 6 3 6 6 11 19 24 7 37 19 1 Cavity 1 only 1.8 MV typical Many trips in Run 1 to find acceptable voltage Cavity 3 Installed 2008-1 2008-3 2008-5 2008-7 2008-9 2009-2 2009-4 Run Number 2009-6 MTBF complete RF System (beam loss only) Beam dumps MTBF year to date 2008 MTBF year to date 2009 MTBF year to date 2010 Overall MTBF STILL dominated by Cavity trips 2009-8 2010-1 2010-3 120 100 2010-5 80 60 40 20 0 2010-1? 2010-2 2010-3 2010-4 2010-5 Partial Run

X-ray count /msv/hr or Power / kw X-ray count / msv/hr Power / kw X-ray count / msv/hr x-ray count / (msv/hr) X-ray measurements on the cavities X-ray count vs Ib 120 100 80 60 40 20 0 X-ray intensity vs Voltage Intensity increases exponentially with voltage 0 0.5 1 1.5 2 2.5 Cavity Voltage (Ib=0)/ MV 30 25 20 15 10 5 0 Intensity varies linearly with power to beam! Fiddled with voltage 0 20 40 60 80 100 120 Beam current / ma X-ray and Power vs Detune (100 ma, 1.4 MV) 140 120 100 80 60 40 20 0-30 -20-10 0 10 20 30 40 Detune angle / (deg) X-ray count Pfor Detuning (i.e. increasing power for constant beam does not change intensity Total intensity is varies with both 140 power and 120 voltage 100 80 60 40 20 0 X-ray count vs Vcav with stored beam @ (100 ma) 1.4 1.5 1.6 1.7 1.8 1.9 2 2.1 Vcav / MV 135 130 125 120 115 110 105 100

LN2 supply pressure stability improved LN2 Supply pressure Peak to peak reduced from ~ 1.5 bar to 0.25 bar Further optimisation likely Tuner position reduced but most noticeable on cavity 1 LN2 Pressure stability improved by the installation of pressure and level control valves on the LN2 supply tank Ongoing investigation to determine residual perturbation

Cavity 2 Failure Cavities 1 and 2 installed and being warmed up over Christmas. Warming up the cavities requires the use of electrical heaters. Procedure and Manual did not include turning off heaters. Heaters were not interlocked. Heaters were left on! First sign: Leak from helium can to insulation vacuum 500 K 400 K 515ºC 460ºC Estimate of max heater temperature 200 K 0 K Maximum EPICS value Heaters OFF CLTS on Cavity 2 Fail

Cavity 2 Failure Investigation revealed: Both Helium level sensors not functioning Main pickup and waveguide coax cables have short circuit (both in helium can). Some of the temperature sensors on the niobium cell have been unsoldered. Helium level probes with blue plastic insulation which has melted Vacuum seal has failed and indium has melted

Cavity 2 Failure Additional observations not related to the increase in temperature Bellow section has distorted. Radial groove from original BCP etch

Copper Plating Problems Peeling copper plating on most pickups and missing plating inside the cups Marks on copper plating in the waveguide. Staining or tracking marks? Damaged plating in waveguide section

Copper Plating Problems Discolouration of waveguide components and of the gasket Staining or damaged plating in the corners of the waveguide

5-8 January: Cavity 2 removed from tunnel and make up vessel installed. 9-10 January: Cavity 1 cooled down noticed that no level sensors were usable and RF pickup cables short circuited. 10 January (Sunday night): Controlling level by controlling total inventory. RF control via spare RF cable on the beam pipe. 11 January: Machine start-up Then move on to Radiofrequency Test Facility commissioning, cavity installation and conditioning in RFTF.

Conditioning of cavity 3 inside RFTF Initial conditioning in February 2010. Gradual increase in cavity voltage and power dips caused by fast vacuum protection during conditioning can be seen. Power dips caused by fast vacuum protection Cavity voltage Forward power Vacuum spikes during conditioning

Soak test in April. Time scale is kept the same as last slide. Improvement in long term performance can be seen clearly. Cavity voltage RBT taper vacuum Forward power Pump out box vacuum ~ 3 days

Infrared pictures of RF window during conditioning 84KW forward power, cavity on resonance 55KW forward power, detune angle -60degree RF Window 28 degree Window heated up to 30 degree Waveguide walls

Q0 (10^9) Q0 (1e9) 2 Q0 measurement showing Q0 drop at low voltage Q0 measurement 1.2 1 Q0 drop possibly caused by field emission 0.8 0.6 0.4 0.2 Original Specification 0 1.1798135 1.3633327 1.5249236 1.6880237 1.8632531 2.0574732 2.2585668 2.4448395 2.6412452 Cavity voltage (MV) Q0 measurement 1.2 1 0.8 0.6 0.4 0.2 Original Specification 0 0.8 1 1.2 1.4 1.6 1.8 2 2.2 2.4 2.6 2.8 Cavity voltage (MV)

Cavity partial warm up experiment Partial warm up to 28K to release hydrogen. Warm up can help with the vacuum but not necessary the long term performance of the cavity Out gassing during partial warm up Vacuum is better after partial warm up. But many vacuum spikes appeared. Some spikes triggered protection.

PMT signal during conditioning PMT signal showing probe blip PMT Probe Forward power X-ray during the pulse Probe Forward power PMT X-ray spike PMT X-ray starts around 1.5MV. Probe Beam trip X-ray spike and probe blip during a trip Forward power

Probe problem 1. Main probe and e- pickup have failed. 2. Cavity 2 and 3 both suffer probe blips. Cavity 1 under investigation. 3. Probe blips happen with and without beam. 4. Probes don t have blips at the same time. 5. Probe blips don t always trip the beam. 6. Very high amplitude. 7. Not successful to filter it out. (Band pass filter, DC block) 8. Not successful with bias voltage. Cavity Signal Spare pickup Another spare pickup

Observed probe blips kicked off wake field simulation of the RF probes DLS Pickup Pin 6 mm CLS Pickup Pin 1 mm 240 mm beam pipe Port-1 Port-2

Snapshot E-Field at t=1.05 ns for 10 & 3 mm bunches, yz-plane s = 10 mm 10 mm bunch The maximum field value is clamped at 100 V/m in both cases. The field at the DLS pick-up has decayed by the time the bunch passes the CLS pickup and therefore appears to be lower. s = 3 mm 3 mm bunch

DLS Pick-up Thin lines 10 mm bunch The EM signal induced by the beam propagates in many modes through the pick-ups. CLS Pick-up Thick lines For 10 mm bunch the voltage induced between the conductors is very low at 0.003 V for DLS pickup and lower still for CLS design DLS Pick-up 3 mm bunch CLS Pick-up DLS CLS 3 mm bunch ~ 7 V between conductors for 250 ma 600 bunches. DLS probe has 4 x CLS voltage

Frequency content of Voltage Signal s = 10 mm DLS CLS Summary: Diamond beam (σ =3 mm) excites stronger signal in the pick-ups compared to the CLS and CESR (σ=10mm) beams for the same charge. s = 3 mm The DLS Pick-ups have larger diameters and so the signal induced will be stronger. Risk of breakdown and wakefield effects are greater for the DLS pickup but unlikely to be the main reason for our beam trips.

Multipactor simulation of the DLS Cavity & Waveguide Nb RF Window Cu (Plating) Al

To establish TW fields in the waveguide Transmitted Reflected Input Monochromatic Excitation with f = 499.654 MHz

Development of Multipactor, P = 200 kw PIC Solver t = 42 ns t = 122 ns t = 2 ns Exponential growth of number of particles indicate multipactor t = 250 ns t = 498 ns

CST model for Multipactor study near Coupling tongue Coupling tongue Electron Source definition TM010 E field from Eigen mode solver near coupling tongue

Preliminary tracking solver Results Eigen mode field scaled to 1 MV across cavity No exponential growth!

DLS IOT Upgrade from TED to E2V IOTs TED IOT E2V IOT

DLS IOT Upgrade from TED to E2V IOTs Successfully upgraded Systems 1 and 2 from TED to e2v IOTs during Christmas 2009 shutdown Advantages Reduced IOT trips Simple tuning and setup with indexed settings Built in radiation shields no lead required Ion Pump readily recovers vacuum during initial filament start up Differences Cavities built around IOT Cathode at the top inside the input cavity Network analyser not required for tuning

e2v S/N Hrs in user operation IOT11 224-0711 2467 IOT12 290-0939 996 IOT13 211-0647 18976 IOT14 212-0647 18839 Current IOT Operating Hours Hrs (Spares) Hrs (Failed) Status Notes IOT31 289-0938 4269 IOT32 287-0931 4264 IOT33 273-0907 5624 IOT34 288-0935 4265 IOT22 223-0710 15327 Grid emmission Waiting for grid outgassing 210-0647 14853 Suspect Under investigation for tripping IOT21 268-0851 1040 Spare 205-0639 1219 Failed During initial commissioning 222-0710 Spare Unused 269-0904 Spare Unused 277-0909 510 Spare 2009: 19 trips during 4300 operational hours (mostly TED IOTs) 2010: 9 x ISCs: 5 during initial run with new tubes 4 in a quick succession on single IOT

1710 2030 3040 3860 5380 8100 10500 12500 15300 20500 25600 30300 35400 40900 46000 50100 50900 55800 57200 60400 61100 61200 62000 62000 62300 65400 66000 67000 67200 67300 67500 67600 68600 71400 71900 72700 73500 73900 82000 Efficiency (%) HV (kv) Typical Operating Conditions (S/N 268-0851) Pin Pout I b Eff Gain (W) (kw) (A) (%) (db) -35 159 35 2.0 50 23.5-35 234 50 2.6 55 23.31-35 352 80 3.29 67 23.4 80.00 Efficiency During Initial Tune/Set Up (S/N 268-0851) 70.00 60.00 50.00 40.00 30.00 20.00 10.00 Note jagged curve due to changes in tuning during initial set up 0.00 Output Power (W)

Current measurement board affected by change from TED to E2V IOTs Original e2v configuration HVPS Curren Total Body I IOT 1-4 Collector Current Collector cable not connected PSU 0V PSU -36kV Not connected IOT Body I -36kV return Now through IOT Body and HVPS I input

Current measurement board affected by change from TED to E2V IOTs All collector inputs are connected Total IOT current transducer Earth current directed through IOT current transducers Body current components removed

Problem: Speed sensing of the warm turbine has occasionally become erratic without prior warning. Repair: After ensuring that the fibre optic cable was properly mounted, part of the signal conditioning box was changed. The problem reoccurred. The frequency to analogue converter was then replaced. There has been no reoccurrence. Frequency to analogue converter Signal conditioner Fibre optic input

Thank you for your attention